We had a nasty scare last night after our Wednesday night race.  We were
motoring back to the dock - about a half hour trip and I climbed down the
companionway into about 2 inches of bay water.  The bilge was full and
overflowing as we motored along.  Inspection revealed no leaks that i could
see from the engine compartment - shaft log, water pump, muffler and
exhaust and thru hulls were all fine.  I jump up to the head and check all
3 thru hulls there - all dry.

We finally get the auto bilge pump working and pumped all the water out -
and no more leak.  I believe that the float switch may have been stuck.

So here's my theory - under power the 30 MK1 tends to squat and the bilge
outlet is below the water on the stern.  We had had rain the week before
and I had neglected to turn on the manual switch to get out the last of any
water in the bilge - the float switch always leaves a few cupfuls in the
bilge.  I am thinking that while under way with the outlet submerged, the
bilge pump cycled on.  Then - as usual - the remaining water in the hose
flowed back into the bilge.  But this time with the outlet underwater, it
started water siphoning into the boat.

After cleaning it all up I checked it in the morning - and it was dry as
usual.  The bilge hose has a high loop in it but no air  break or check
valve.

I am thinking a check valve or an air break would keep this from happening
again - any opinions would be welcome.

Oh - and I think I will fix the manual bilge pump that I have been putting
off for a while!

thanks,

Joe
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