On 2/24/2025 1:21 PM, robert7721--- via KRnet wrote:
Looks like the original nose gear failed at the lower assembly. The
through-bolt sheared. I am going to take it apart, but not sure I can
fix it.
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Is this an item that everyone with similar setup should check before
next flight? Was the bolt worn? I tried to make it a habit on annual
inspection to rotate any bolt that was capable of rotation such as in
control cable connections. I would give each a 1/4 turn to cut the wear
rate by a factor of 4.
Larry Flesner
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