In the summer of 2010, we fell off a 4 ft wave while close reaching in 16
knots true, and something went POP. Sounded like a .22 going off; and I said
"F***! Something broke!"

 

One of the jump stays between the first and second spreaders, which I later
learned is officially called the D2 shroud, was waving around in the breeze.

 

I'd already given thought to inspecting the 34 year old rod rigging. Now
that something had broken I obviously had to make it a priority.

 

Turns out that the threaded toggle in the turnbuckle used to tension the
shroud had broken. I learned that the recommendation is to replace all the
threaded toggles used in rod rigging every 10 years because of the
possibility of crevice corrosion where the threaded rods are swaged into the
hex in the middle. My rigger also said that dye checking the rod heads would
only identify cracks, but would not identify all causes of failure. Cost of
the dye check would be a bit over $2k with yard fees for unstopping the
mast.

 

For a full inspection of the old rod, it would need to be removed, packed,
and shipped to Navtec for testing. Cost would be about $3500, plus any
reheading or replacement based on the outcome of the testing.

 

For about the same cost as the inspection of the rod, I replaced the whole
standing rigging with Dyform wire. The wire is a scoosh larger in diameter
(about 1/16th) than the #10 rod being replaced, but the break strength of
the wire is actually higher than the strength of the rod being replaced. The
upper end of the wire uses swaged fittings that fit the ball sockets of the
rod rigging (so no mast tang changes), and the lower fittings are Stalocks.
I changed the deck level turnbuckles to open style to make adjustment
easier. On the diagonals, I retained the internal style turnbuckles and
replaced all the toggles so I would not need to change any of the joint
fittings on the end of the spreaders.  Another advantage of the change to a
wire headstay was that it allowed me to install the Bamar roller furler ;
Bamar does not recommend having a roller on rod rigging because dirt in the
bearings can scratch the rod and create a stress riser that weakens the rod.

 

BTW, the ends of my spreaders were also corroded, but not so much they could
not be cleaned up and reused. I changed over to leather spreader boots that
are sewn on, instead of the nylon pads that were put on in 2003. My rigger
thought the leather boots will allow better flushing by rain water and
better airflow to prevent corrosion of the aluminum ends of the spreaders.

 

 

Rick Brass

Washington, NC

 

 

-----Original Message-----
From: David Folsom < <mailto:dfolsom...@gmail.com> dfolsom...@gmail.com>
To: cnc-list < <mailto:cnc-list@cnc-list.com> cnc-list@cnc-list.com>
Sent: Mon, Jan 21, 2013 2:41 pm
Subject: Stus-List Replacing Spreaders and Standing Rigging

Hi fellow C&C owners. 

 

 

Can anyone tell me about their experience with replacing their standing
rigging?

 

thanks

 

Dave Folsom

1981 C&C 36 Rebel Maid

San Diego

 

 
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