On Thursday 24 January 2019 21:52:23 Jon Elson wrote:

> On Thursday 24 January 2019 08:41:47 Todd Zuercher wrote:
> >> I have a fair amount of experience with high speed spindles.  And
> >> I've found that most are incapable of running much below about 1/3
> >> of their rated speed for any length of time, and cutting anything
> >> at those speeds is certainly out of the question.  If you don't
> >> believe me, start your 18k rpm spindle at 4000rpm and then check
> >> the current readout display on the VFD, and you will be shocked at
> >> what numbers you see displayed (I'd venture a guess that it would
> >> be close to about 200% of rated amps on the motor name plate).
>
> This would indicate the Volts/Hz ratio is not set right.
> This might make the spindle accelerate better, but if set up
> properly, you should not see excessive current at low
> speeds.  Some drives have multiple breakpoints, so the V/Hz
> curve can have multiple slopes between those points.
>
> We have a really off-brand mill at work that has an 18000
> RPM spindle.  You can run it all day at 1000 RPM with no
> heating.  It really lacks torque at all speeds, obviously
> designed for high speed, but won't burn anything up.
>
> Jon
>
I found some programing info that made it work, but just one more problem 
leads to another and I'm beginning to wonder if I'll ever find the last 
one. I hadn't noticed it was running backwards, and that wiring was 100% 
OEM.  So tonight I opened the box again to reverse two of the motor 
wires.  But while in there I decided to put the box on a diet as its 
about 40 lbs.  So I got rid of the 4 TB6560 drivers, and a surprisingly 
heavy power supply that ran them, leaving just the vfd, the breakout, 
and a smallish fan.  Got it all back together and found the fan was 
quiet. Seems it was plugged into the BoB which was plugged into the PSU 
I took out. Ooops! The PSU I took out must have been running in foldback 
as it was  making 14 volts when I checked it with all steppers powered 
up, but it was marked 24 volts at not enough current for 4 steppers when 
I finally uncovered the label. So I gave up for the night, not finding a 
psu to run the fan with. I have some boosters on order, and a small 5 
volt supply I can put back in it to run the booster to get something 
like 25 volts to run the fan. Then see if I can make reverse work, once 
I get it turning the right direction. Theres a couple registers in it 
that might control that, or I may have to fiddle with my hal. It clearly 
has a control terminal labeled REV so I am determined to make it work.

The right sized 4mm mills came in today, so once it spins the right 
direction, I'll go get me a spoil board and carve the panels for 2 new 
control boxes.  Then I'll have enough I/O to put some home and limit 
switches on it. 

Mechanically this machine is very solid, backlash a thou or less, and 
with 28 solid volts for the motors, is easily running 100 ipm for 
rapids. And this is with software stepping! I think I'm going to like it 
except for the 3" Z range. I'd like 6 so I could do some real carving...

Thanks Jon.

Cheers, Gene Heskett
-- 
"There are four boxes to be used in defense of liberty:
 soap, ballot, jury, and ammo. Please use in that order."
-Ed Howdershelt (Author)
Genes Web page <http://geneslinuxbox.net:6309/gene>



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