Jeff, 

I called Dan Diehl and he was kind enough to chat with me for 10 minutes or so. 

The issue he had with the motor was aftermarket head studs. He would use 35" 
for takeoff, 28" in cruise and had run it up to 50" for short bursts. After 
putting OEM 8mm studs on it, he did not have another problem. 

Thanks for the tip!

Jeff Lange

On Mar 25, 2013, at 12:58 PM, "Jeff Scott" <jscott.planes at gmx.com> wrote:

> The prototype KR2s Joe is referring to was Roy Marsh's plane, N133RM.  Last I 
> heard, Roy was living in California, although the plane has changed hands a 
> couple of times since then.  Last I knew it was also in California.
> 
> Seems to me that Dan Diehl ran a turbo VW in N4DD for a while as well, so may 
> have some useful information.
> 
> Sounds like you are taking a sound approach with this.  Congratulations on 
> the fine work.
> 
> -Jeff Scott
> Los Alamos, NM


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