Thanks, I do have an isolating transformer as well, so I will use that. I have 
done previous tests with a bench PSU on the UC3842 and found it needs 16V to 
get going. I just checked the Technical Description and it says the minimum 
current on the 5V output is 6.4A and on 12V it is 0.17A. I checked my load 
board and it is only going to sink 3A, so I need more load as I think the IDE 
disk is not going to be much. Would insufficient load really cause it to 
shutdown so quickly though?

 

Not sure I understand your comment about “designators for networks”, is there 
an example you can point me at? One of the things I have tried to do, but 
clearly not very successfully, is to minimise the lengths of the wires.

 

Regards

 

Rob

 

From: Mattis Lind <mattisl...@gmail.com> 
Sent: 29 March 2020 08:51
To: r...@jarratt.me.uk
Cc: General Discussion: On-Topic and Off-Topic Posts <cctalk@classiccmp.org>
Subject: Re: VAXmate PSU

 

Hello Rob,

söndag 29 mars 2020 skrev Rob Jarratt <robert.jarr...@ntlworld.com 
<mailto:robert.jarr...@ntlworld.com> >:

Thanks Mattis. I do test it with a load, although to be honest I forgot to do 
this when I took the measurements yesterday. I use a modern-ish IDE disk and a 
load board from a MicroVAX 2000 as the dummy load. I don’t know if that is 
sufficient.

 

Do you know the nominal output rating for the supply?

It might be the case that even with load board the load is uneven. But it 
sounds less likely.  

 

I don’t know enough about PSUs to make the secondary side drawing more logical 
unfortunately.

 

Can be hard. But a good idea is try to minimise the length of wires. Maybe use 
designators for networks instead of wires to make the schematic more readable. 
On the other hand I was reading the post on the iPad. 

 

I have a variac and a bench power supply, so I could do what you suggest. 

To stay safe you need a protection transformer as well. Otherwise the the bench 
supply will end up at line potential. With the protection transformer in place 
the circuit will be left floating in relation to earth. With a variac you can 
then vary the input and keep it within safe limits. If you don’t have a 
protection transformer and variac then another bench DC supply that can give up 
to 100 V can be used instead. 

 

Could you be a bit more specific about where to apply what, so I don’t do it 
wrong or damage something? Would you put the bench PSU across the UC3842 Vcc 
and Gnd pins? I am not sure what would happen if the normal supply to the 
UC3842 was still in place with the bench power supply also trying to supply 
power. Would it be wise to lift R32 so nothing conflicts with the bench power 
supply? 

 

Absolutely right. I should have been more explicit about where to introduce 
external supply. But as you say, lift R32 to isolate the switching controller 
and feed in the bench supply current at VCC. Check the data sheet for what is 
approriate voltage. 

 

Good luck!

 

/Mattis

 

Thanks

 

Rob

 

From: Mattis Lind < <mailto:mattisl...@gmail.com> mattisl...@gmail.com> 
Sent: 29 March 2020 06:39
To:  <mailto:r...@jarratt.me.uk> r...@jarratt.me.uk; Rob Jarratt < 
<mailto:robert.jarr...@ntlworld.com> robert.jarr...@ntlworld.com>; General 
Discussion: On-Topic and Off-Topic Posts < <mailto:cctalk@classiccmp.org> 
cctalk@classiccmp.org>
Subject: Re: VAXmate PSU

 

Hello Rob,

lördag 28 mars 2020 skrev Rob Jarratt via cctalk <cctalk@classiccmp.org 
<mailto:cctalk@classiccmp.org> >:

I have posted here a couple of times because I have a failed VAXmate PSU. I
have just posted a little bit more information here:
https://robs-old-computers.com/2020/03/28/further-analysis-of-the-vaxmate-h7 
<https://robs-old-computers.com/2020/03/28/further-analysis-of-the-vaxmate-h7270-psu-failure/>
 
270-psu-failure/ with some scope traces and a greatly improved schematic.
Although the schematic is likely to have errors still. Unfortunately, a
stray scope probe ground lead blew the fuse so now I have to wait for a new
fuse to arrive before I can continue work.



I would really like to know if all the spiking I am seeing is to be
expected, and any suggestions why it appears to be detecting an overcurrent?
There do not appear to be any shorts on the secondary side, but that could
be wrong of course. I don't know if a genuine short anywhere would cause it
to trip the SCR quite so quickly (within 20ms of the switching transistor
starting to switch).

 

This is fly back design and I would expect some spiking when the transistor 
shuts off.  

 

Then for over-current. It might be so that there are over-voltage protection on 
the outputs that kicks in. A crowbar that short circuits the output. It looks 
like there is such a circuit on 5 and 12 V. But to be honest the output circuit 
schematic is hard to read. 

 

If you have no load or little load or un-even load the PSU might hae problems 
to regulate. I know for fact that the PSU in the MicroVAX 2000 need to have a 
dummy load when no hard drive is installed otherwise there will be uneven load 
which it has hard time to handle sonce the output regulation is based on the 
sum of the outputs somehow. It will trip the crowbar on over voltage on one of 
the outputs otherwise. 

 

What if you supply the control circuitry on the primary side using a bench lab 
supply and then connect a protection transformer and a variac in series to the 
normal AC inlet. 

 

Slowly increase input AC voltage while monitoring source voltage and output 
voltages.  At what AC input voltages does it trip? What is the output voltages 
at this point? 

 

If both voltages exceed normal and the crowbar trips I would think that the 
feedback network somehow reports to low output voltage to the control 
circuitry. Maybe the opto coupler is bad?

 

Sorry. A lot of guessing here. But it is hard to tell withour more 
measurements. 

 

/Mattis

 



Any thoughts gratefully received.



Thanks



Rob

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