here's the output from sudo /opt/scripts/tools/version.sh git:/opt/scripts/:[1aa73453b2c980b75e31e83dab7dd8b6696f10c7] eeprom:[A335BNLTBLA21717EL001649] model:[TI_AM335x_BeagleBone_Blue] dogtag:[BeagleBoard.org Debian Image 2018-10-07] bootloader:[eMMC-(default)]:[/dev/mmcblk1]:[U-Boot 2018.09-00002-g0b54a51eee]:[location: dd MBR] kernel:[4.14.71-ti-r80] nodejs:[v6.14.4] uboot_overlay_options:[enable_uboot_overlays=1] uboot_overlay_options:[uboot_overlay_pru=/lib/firmware/AM335X-PRU-RPROC-4-14-TI-00A0.dtbo] uboot_overlay_options:[enable_uboot_cape_universal=1] pkg check: to individually upgrade run: [sudo apt install --only-upgrade <pkg>] pkg:[bb-cape-overlays]:[4.4.20180928.0-0rcnee0~stretch+20180928] pkg:[bb-wl18xx-firmware]:[1.20180517-0rcnee0~stretch+20180517] pkg:[kmod]:[23-2rcnee1~stretch+20171005] pkg:[librobotcontrol]:[1.0.3-git20181005.0-0rcnee0~stretch+20181005] pkg:[firmware-ti-connectivity]:[20170823-1rcnee1~stretch+20180328] groups:[debian : debian adm kmem dialout cdrom floppy audio dip video plugdev users systemd-journal i2c bluetooth netdev cloud9ide gpio pwm eqep admin spi tisdk weston-launch xenomai] cmdline:[console=ttyO0,115200n8 bone_capemgr.uboot_capemgr_enabled=1 root=/dev/mmcblk1p1 ro rootfstype=ext4 rootwait coherent_pool=1M net.ifnames=0 quiet] dmesg | grep pinctrl-single [ 1.070379] pinctrl-single 44e10800.pinmux: 142 pins at pa f9e10800 size 568 dmesg | grep gpio-of-helper
Also here's systemct status: systemctl status robotcontrol.service ● robotcontrol.service - robotcontrol Loaded: loaded (/lib/systemd/system/robotcontrol.service; enabled; vendor preset: enabled) Active: failed (Result: exit-code) since Sun 2018-10-07 16:51:01 UTC; 1min 14s ago Process: 1533 ExecStartPre=/usr/bin/rc_startup_routine (code=exited, status=255) Oct 07 16:51:01 beaglebone systemd[1]: Starting robotcontrol... Oct 07 16:51:01 beaglebone rc_startup_routine[1533]: timeout reached while waiting for pwm drive Oct 07 16:51:01 beaglebone rc_startup_routine[1533]: TIMEOUT REACHED Oct 07 16:51:01 beaglebone systemd[1]: robotcontrol.service: Control process exited, code=exited Oct 07 16:51:01 beaglebone systemd[1]: Failed to start robotcontrol. Oct 07 16:51:01 beaglebone systemd[1]: robotcontrol.service: Unit entered failed state. Oct 07 16:51:01 beaglebone systemd[1]: robotcontrol.service: Failed with result 'exit-code'. thank you, Scott On Tuesday, March 26, 2019 at 8:26:51 PM UTC-4, RobertCNelson wrote: > > On Tue, Mar 26, 2019 at 7:15 PM <[email protected] <javascript:>> > wrote: > > > > I guess I need to give more details. I’m using the eduMips platform. It > looks like it’s failing to start the PWM module. I’ve seen some postings > related to PWM but I can’t seem to find a solution. > > Let's see: > > sudo /opt/scripts/tools/version.sh > > Regards, > > > -- > Robert Nelson > https://rcn-ee.com/ > -- For more options, visit http://beagleboard.org/discuss --- You received this message because you are subscribed to the Google Groups "BeagleBoard" group. To unsubscribe from this group and stop receiving emails from it, send an email to [email protected]. To view this discussion on the web visit https://groups.google.com/d/msgid/beagleboard/ef90c72e-3ff1-40cc-a1e5-340491e412cd%40googlegroups.com. For more options, visit https://groups.google.com/d/optout.
